White car:
We had a lot of breakup due to the MSD not working, so we only made 444rwhp @ 8.8psi @ a low 6200rpms. The car was pulling REALLY strong after 5500rpm's. It looks like we would have made 515-530 @ 10psi @ 7000rpm's.
We pegged the 42lbs injectors at 420rwhp so we are now running 52psi base fuel pressure.
I Think there is a 9 second run in the car with a 100 shot out of the hole if we can get a 1.4 60ft time. This will only happen if we go to Norwalk or Bowling green and if the Raxle halfshafts cooperate. Overall the car feels very strong on the street.
Red Whore:
Things weren't looking good as I pegged the 24lb injectors on the second pull @ 5600rpm's ~285rwhp. The rest of the pull went lean.
Finally with 50psi base pressure we could get the a/f ratio correct until 6500.
Best pull was 308hp/265tq. The intake leveled off at 6300rpm's, a little sooner than I thought. This intake is only 2" shorter on the runners. I think I will pull another 25rwhp with the next intake and bigger fuel injectors I put on the car. Getting 330-335 will not be a problem on pump gas.
We worked on drivability sorted and did only pulls adding fuel, and timing in some spots. We did not spend anytime at all on this car, except for the idling. It seems to be tough to get these cars with 235+ degrees of duration to idle correctly.
I also have a lot of oil blowby, possibly a piston ring on the drivers side. I will get this sorted out, install the new intake etc when I get time this year and should make 330-350 through a 4R70W and stock bottom end which will be fantastic!
We will have at least John's car at test and tune this Saturday if the weather cooperates. I do not know if I will bring the red whore out or not.